Dive Log:  2005

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Date: 17 Apr 05
Wx: Clear, winds SW 10-12 kts, high 72F
Seas: About a foot and a little choppy
Viz: 20 ft near the bottom
Temp: 68F on the top, will check the computer later

This was our first dive after replacing the fuel tank and rewiring the boat.  We took tanks for 3 dives, but we were so cold after the first dive that we put on our dry clothes and just enjoyed a day on the water.  I think the long lay-off affected our stamina.  We went to a shallow reef (Anniversary) so Candy could try out a new drysuit.  She didn’t have any major problems, just the usual weight and buoyancy issues with a new suit.  We didn’t see anything legal for the first 25 minutes, but I shot a nice Red Snapper and Trigger just before we had to go up the line. I used a new
JBL Woody Magnum.  I only cocked two bands, but that was more than I needed.  Tomorrow (19 April 05), we will be looking for bigger game.

 

The boat is running great.  The only problem was with my freshwater pump which failed after three years.  Candy ordered a new one (18 April) and I installed it the same day.

 

Date: 19 Apr 05
Wx: Partly Cloudy, then Clear, winds SE 15 kts, high 72F
Seas: 3 to 4 ft
Viz: 50 ft out deep, 20 ft inshore
Temp: 68F on the top, 65F below

 

The Navy Wave Model and the Marine Forecast were bogus.  Should have been variable winds 10 knots or less, and seas about a foot.  By the time we were 10 miles south of the Pass, the wind was steady at about 15 knots out of the southeast.  We got knocked around pretty good.  We left the dock at 0850 and returned at 1830.

 

Dive One:  Angelina.  Candy had a mask flood and motioned for me to dive solo.  Vis was about 50 ft.  I worked my way down from the wheel house.  Didn’t see anything legal for the first 10 minutes.  I finally took a look under the stern and saw a nice Red Grouper - 31 inches, and about 25 pounds (the scale broke while I was weighing it).  Candy’s mask turned out to be broken right at the bridge of the nose.  That’s why we keep spares on the boat.

 

Dive Two:  Deborah.  This wreck is less than two miles from the Angelina, so the conditions were the same.  Candy used her backup mask, but by the time we hit bottom, she found out her BC wasn’t holding air.  We were surrounded by AJs that were just under legal.  I never took a shot.

 

Dive Three:  Janet.  I wanted to see the LCM-8 sitting upright, but there was a boat on it.  We didn’t fix Candy’s BC problem, but we have had a similar problem before.  When Candy got to the deck of the wreck, she removed one weight pocket and left it next to the anchor line.  She was fairly neutral for the rest of the dive.  The vis was 20 ft or less.  We had the same “less than legal” AJs all over us.  I finally made it down under the bow (the bottom is at 103 ft after Ivan scoured the sand away).  Saw a lobster sitting in the sand under some old anchor rope.  As I went to grab him, he took off, but he hung up on a piece of monofilament and I grabbed him out of midwater.

 

I am really glad to be carrying a lift bag on every dive.  This time, I dropped the anchor past the wreck and drifted back over it.  The anchor line was fouled in some of the structure, so it would not have been easy to just motor forward over the wreck and use the anchor ball.  I used the lift bag to get the anchor up and over to the down-current side of the wreck.  Candy dumped some of the air out of the lift bag so we wouldn’t drift into the boat anchored on the LCM-8, then we used the anchor ball as usual.

 

Except for getting beat up by the 3-4 ft seas, it was great being back in the water.  Boat ran great again, and the new fresh water pump is working super.

 

Date: 2 May 05
Wx: Clear, winds NE 10-20 kts, 60’s in the morning high 72F
Seas: Less than a foot in the bay, about 3 ft offshore
Viz: 5 - 20 ft
Temp: Water is still pretty cool, will check the computer later

 

Navy Wave Model was fairly accurate.  Marine forecast was off by a couple of hours.  We shoved off about 0830.  The northeast wind was still cranked up.  We thought about Baskins Barge, then decided to drop by the LCM-8 first.  By the time we were a couple of miles offshore, we were into 3 ft waves and whitecaps.  Wind was not the predicted 10 kts, more like 15 -20 kts.  We decided to get as close to shore as possible.

 

Dive One:  Miss Louise.  Yes, the Miss Louise.  I hate that wreck.  Vis on one side of the boat was 10 – 15 ft.  Vis on the other side was 5 ft.  I saw the shadow of very large fish.  Candy told me later that it was a big grouper.  Never pulled the trigger.  Neverlost flooded.

 

Dive Two:  Air Force Barge.  Another wreck I will only dive if I am forced inshore.  Fortunately, it held red snapper.  I shot a big sow that spun off.  Candy shot 2 more, then I shot about a 27 incher.  My shaft broke at the weld near the notches.  It must have had a defect.

 

Candy tried out her new back plate and wings.  Buoyancy control was fine and the streamlining is much better than her old SeaQuest.  It will take a couple of dives for her to get use to the new placement of gear.

 

We bought a “Sun Shower”.  It’s a 4-5 gallon bag that heats water when you lay it in the sun.  Water hit 104 degrees and felt great going down the wetsuit.

 

Boat continues to run great.

 

Date: 7 May 05
Wx: Clear, winds SE 10-12 kts, 54F in the morning high
72F
Seas
: Less than a foot on the way out, but two feet and a little choppy on the way home
Viz:  The viz is so variable, I’m going to report it only for each site

Temp: 68F on the top, will check the computer later

 

0720 arrival at the Marina to load the boat.  Had great help from our buddy Jim.  We haven’t dived together since the effects of Ivan abated somewhat in November 2004.  We headed straight for wreck alley (the Belize Queen).  When we arrived, the whole area looked like a boat parking lot.  As luck would have it, the boat on the Belize Queen belonged to a friend.  We tied off to his stern and got ready to dive.  We were hailed by Snake 166 at about the same time, and saw him off our port.

 

Dive One:  Belize Queen.  Seas were calm, almost no current.  Since we were tied to the stern of another boat, we had to make a longer swim than normal.  Vis was about 20-25 ft.  We only saw triggers and short AJs.  We took 3 triggers and headed back up.  At the safety stop, I dropped my new gun (JBL Woody Magnum).  After I got back on the boat, I lowered my anchor so that when the other boat departed, I could hold my position and look for my gun (which shouldn’t be too far from my anchor).

 

Dive Two (for Stone and Jim):  After the surface interval, my buddy and I headed down.  I tied off a reel line to the anchor chain and started a circular search.  I found the gun about 60 ft from my anchor as I started the second circle.  Best sand dive I ever made.  I also encountered some of the old wheelhouse, but it is just scrap that is too small to be seen on a bottom finder. 

 

Dive Two (for Candy):  After driving around the boat parking lot for a while, we found the Odyssey open (probably because it is beat to death and has very little relief).  Candy did a solo dive, but did not pull the trigger.

 

Dive Three:  Tried to hit an old spot.  The anchor chain fouled the flukes, but we didn’t know until it was too late.  Candy was first to the anchor.  She un-fouled the flukes, and set the anchor in the sand (mud).  We hit the water with the GPS showing .03 miles (which is normal for scope at that depth).  I made it to the edge of the site after swimming 150/200? ft.  We didn’t have time to investigate.  Back on the boat, the GPS told us we were about .08 of a mile from the site.

 

Epilogue:  While telling my buddy about replacing the fuel tank, rewiring most of the boat, and replacing vents, the holding tank, and the trim tab hydraulic unit . . .  I also mentioned that I dropped a hatch cover on the distributor cap (which I replaced).  Since my boat has never run this good, I am now leaning toward the theory that my old distributor cap was to blame.

 

Date: 12 May 05
Wx: Clear, winds SE 10-15 kts, 70F in the morning, high
80F
Seas
: About 2 ft and choppy on the way out. 3 ft and very choppy on the way home
Temp: 74F on the top. Starting to notice a little bit of a thermocline.

Got out of the marina by 0900. The wave model predicted 1 ft seas. The Marine forecast predicted winds less than 10 kts and variable in the morning. They were wrong. Even at 0900 the winds were over 10 and steady out of the southeast.

Dive One: We dropped anchor on the Angelina. We even threw out the tag line with anchor ball attached. I called the dive before gearing up due to a massive surface current. Tried the Awesome next. There was still quite a current, but it was not as bad.
Vis was pretty good, maybe 35 ft. Not much left of the wreck which sits in a hole at 124 ft. Just 100ft from the wreck, the depth is only 95 ft. Candy shot a trigger.

Dive Two:  Started to dive the Destin
Liberty Ship, but a boat beat me to it and started trolling. We headed to the Barrel Barge and got one more dive in. It’s weird diving a shallow wreck and getting 45 minutes of bottom time. Candy and I have gotten use to 15-20 minute bottom times on the deeper wrecks. Candy shot a flounder.

By the time we headed in around 1600, the seas were 3 ft and I was headed east into a southeast wind and swell. I got a little wet.

Boat continues to run great.

 

Date: 14 May 05
Wx: Clear, winds SE 10-15 kts, 65F in the morning, high
80F
Seas
: About 2 ft and choppy on the way out.  3 to 4 ft swell and a little choppy all day
Temp: 74F on the top.  Still 68F on the bottom (135 ft)

 

Got an earlier start today.  Met Subdude and Jim at the marina at 0630 and shoved off at 0710.  Boggy Bayou was nice and flat.  The Bay started building on the way to the pass.  The Gulf had a SE swell that started out about 2 ft, but was easily 3 ft by the time we reached our first site.  The swell period was not too short, so it wasn’t terrible.

 

Dive One:  Jim and Subdude.  Tried to find the Valp #2 boat.  Didn’t see anything exactly on the old numbers, but saw a little relief within .01 miles.  I apparently dropped the anchor between what is left of the boat and some of the culverts in the area.  Subdude may give more details, but he said the boat is broken up.  I think the vis was 30 ft.

 

Dive One:  Prewitt Tug.  Tug has moved due to Ivan.  I will post the new coordinates in the ECRA member’s forum.  I drove over the old numbers twice and saw nothing.  After about 10 minutes of “freehand” searching, we started preparing a marker buoy to start an “organized” search.  I put the boat in idle, but kept my eye on the bottom finder.  Before we had a chance to throw the buoy overboard, we drifted over the wreck.  The surface current was pretty strong, but we had 2 up and 2 down, so we weren’t as worried.  The Prewitt is still upright and in fine condition.  Many schools of AJ, but 99% were short.  As soon as we hit the deck, we saw a Goliath Grouper which was less than 5 ft (I use Candy as my ruler), several large ‘cudas, and a few red snapper.  I shot a lonely red grouper.  Vis was about 30 ft.

 

Dive Two:  Prewitt Tug again.  We were hoping for some legal AJs to visit, but no luck.  I shot a red snapper.

 

We considered a third dive on the Janet or LCM-8, but the seas were still building and the following swell was pushing the boat around like a drunken sailor.  Getting through the pass was fun!

 

Boat ran great, but the main bilge pump was intermittent.  I’ll probably buy a new pump, then work on the old one.

 

If anyone needs marine stuff, let us know.  Candy is a dealer in discounted name brand marine parts and equipment.  She can get really good prices on quite a few boat parts & accessories.

 

Date: 21 May 05 (ECRA Fishing/Spearfishing Tournament)
Wx: Clear, winds N 10-15 kts early, 70F in the morning, high 80F
Seas: Less than 2 ft inshore, but there was a 3 to 4 ft swell out of the SW offshore
Temp: 74F on the top.  Still 68F on the bottom (135 ft)

 

I loaded most of the gear on the boat the night before.  We left the house at 0430, and left the dock a little after 0500.  Lightning was over Destin while it was still dark, and as the sun rose, we could see the storm front.  After clearing the Pass and determining the swell and wind conditions, we headed SSW.

 

Dive One:  Deborah.  For the first time ever, we beat the fishing boats to a site.  First anchor drop didn’t catch, so we pulled it and tried again.  Strong North wind against a 3-4 ft SW swell made for a rocking boat and difficult gear-up and entry.  There was a fairly strong surface current, so we increased the tag line to about 150 ft.  The Deborah is upside down, so there is no superstructure to hold fish.  If the AJs don’t come to visit, then you have to look for fish with your belly in the sand which is at 135 ft.  Vis was about 30 ft.  We never pulled the trigger.

 

Dive Two:  Angelina.  We made the dive a little over an hour after the Deborah.  I didn’t see any fish in the superstructure, so I went to the sand again (135 ft).  Shot one red snapper, but had to call the dive when I went into Deco (Candy went into Deco a minute later).  Had a beautiful spotted dolphin visit us on the surface, and on the way to the next site, I saw what looked like a squadron of turtles just under the surface.

 

Dive Three:  FWB-Butler-Brown Barge.  After Deco diving, we needed to move inshore for some shallower dives.  Drove by the Destin Liberty Ship (boat parking lot) and over to the Reefex Tank area.  There were boats on all the tanks, too.  We ran over to the FWB barge just as a boat moved out of the area.  The barge has moved and I will post the numbers in the ECRA member’s forum.  The top of the barge use to be fairly intact, but many of the deck plates and side plates were disintegrated by Ivan.  Candy saw a Goliath Grouper. . . probably the reason for no fish on the barge.

 

Dive Four:  The boats in the Reefex area had departed, so we went to the tank we had first tried to dive.  Vis was about 20 ft.  I shot a grouper.  Candy shot some triggers, a nice black snapper, and a flounder.  Unfortunately, Candy’s shaft got wedged in the tank.  We spent the surface interval attaching another shaft and lanyard to her gun.

 

Dive Five:  We didn’t have much time to look for another site before the tournament weigh-in, so we stayed on the tank for our last dive.  We got skunked.

 

Epilogue:  We made it to the weigh-in at AJ’s with 15 minutes to spare.  The fish fry and awards ceremony was a lot of fun.  Candy’s flounder earned her first place in the lady spearfisher division (she was also the only lady spearfisher).  I picked up second place in the Gag Grouper and Red Snapper spearfishing categories.

 

We motored back home through a one-foot chop on the bay, but the moon was almost full and the vis was good (I’m still glad I have radar).  At one point I saw a shrimp boat dead ahead, but I could only see his stern light, so I thought I was following him.  As I got closer, I could see that I was approaching him from his port, so I maneuvered around him.  Turns out, his port lights were not working.

 

We made home port about 10 pm and called it a night.

 

Date: 28 May 05

Wx: Clear, winds West to WSW, 70F in the morning, high 80s F
Seas: Big swell out of the SW.  Started white-capping in the afternoon
Temp: 79F on the top.
  Still 68F on the bottom

 

We were on the bayou by 0630.  Bay was fairly calm

 

Dive One:  Hit an old wreck that was pretty beat up by Ivan.  It sits in a hole, so what little structure is left is about level with the seafloor.  The bottom finder shows no relief, but I was able to see a change in the density of the bottom.  I shot two nice black snappers (24 inches) and a trigger.  Candy shot a red snapper and a trigger.  Vis was about 20 ft.

 

Dive Two:  Same wreck. . . more triggers.

 

Dive Three:  Another wreck.  Vis was at least 40 ft horizontal, and I could see the bottom at 50 ft vertical.  Nice dive but no fish.

 

We were going to retrieve Candy’s spear, but there was a boat on the tank.

 

Date: 29 May 05

Wx: Overcast early, then clear.  Winds West to WSW, 70F in the morning, high 80s F
Seas: Swell still out of the SW, but smaller and less wind
Temp: 79F on the top.  Still 69F on the bottom

 

We were on the bayou by 0630.  Bay was nearly flat.  Marine forecast called for 2-3 ft seas, but this time they were off by 6 hours in our favor.  The seas actually calmed between 0630 and 1230.  Current on all sites was non-existent.  The end of the granny line that attaches to the anchor line was dropping down about 50 ft, so after stepping off the dive platform, each descent was almost straight down to the site.  After burning many $$ on offshore excursions, we decided to stay close. 

 

Dive One:  Went to the tank that swallowed Candy’s spear during the ECRA tournament.  I took a boat hook down with me and managed to retrieve the spear after 10 minutes of effort.  Vis was only 10 ft and Candy got a single trigger.

 

Dive Two:  Went to another tank.  Same bad vis and a couple more triggers.

 

Dive Three:  Hard bottom.  Vis was better, maybe 20 ft.  Candy took the line-reel.  I found a nice, large shell as soon as we hit bottom.  All the fish were short.  One lobster.  The anchor was in the sand, but there were rocks in every direction.  I’ve said it before:  The lift bag goes on every dive.  In a low current situation, I can hook the bag to the anchor shank and add enough air to float the anchor.  The weight of the chain keeps the anchor from heading to the surface.  Once on board, a few pulls on the anchor line and the lift bag pulls the anchor straight up out of the surrounding rocks.

 

I got Candy’s spear back, but broke a tip (a better than even trade).  We were finished diving by 1230.  Took a hot shower courtesy of the “Sun Shower” laid out on the hard-top, got into dry clothes, and made a leisurely (gas friendly) run back to port.  Wind and seas were building the whole time, so we finally got lucky with our timing.

 

Date: 4 Jun 05

Wx: Clear and partly cloudy.  Winds SE, 70F in the morning, high 80s F
Seas: Swell out of the SW.  Mostly 3-4 ft.
Temp: Warming up - 74F on the bottom

 

Got to the marina by 0600 and we were in the bayou by 0635.  Buddies were Candy and Jim.  One minute after clearing the Pass, the temperature gauge shot to 240 F and the alternator gauge dropped below 12 volts.  I chopped the throttle and turned back to get into the snorkeler’s jetty.  The temp and alt gauges returned to normal almost immediately and there were no other signs of overheating, so we assumed it was a sensor or electrical problem.  Marine forecast was pretty close.  There were more 4 ft swells than 2 ft swell.  The SE wind and the SW swell made for painful rocking.

 

Dive One:  Broken Bottom.  Due to sea conditions, we decided to stay inshore.  Nice dive, but this site must get fished a lot.  I used a new 5-mil Hyperstretch instead of my 7/5 Goldcore. . . much more comfortable and easy to get into.  Surface current was a little strong, and there was some current on the bottom.  Vis was about 20 ft.

 

On the way to the next site, the engine temp shot up again.  This time we opened the hatch and removed the cabin steps to see what we could see.  While I moved the throttle from idle to higher RPMs, Jim checked out the belts that run the alternator, seawater pump, and block pump.  Jim discovered that at higher RPMs, the pulley on the block pump was not keeping up.  He tightened up the belt and we were good to go for the rest of the day.

 

Dive Two:  More broken bottom.  The vis on top was at least 50 ft, but the bottom was only 15 ft.  Candy clipped off a line reel to the anchor line, but it fouled and we took a long time to fix it.  I took Candy’s under-powered gun on this dive because I didn’t expect to see any real action.  The first fish I saw was a 20 lb grouper.  I couldn’t even try the shot with the short gun.  I got a trigger and a couple of lobsters.

 

Dive Three:  We stayed on the same site so I could take down the big gun to get the grouper.  Strangely, there were very few fish.  Ten minutes into the dive we found out why.  Two bull sharks were patrolling.  One was only 5 ft, but the other one was about 8 ft.  Candy picked up some nice shells and I picked up some lead.

 

Epilogue:   Made it back to the Pass by about 1600.  SW swell was meeting outgoing tide, so the Pass was a washing machine with 4-6 ft waves going in every direction. . . always an adventure!  Bay was pretty choppy, but not white-capping.  Back in port by 1630.

 

Date: 14 Jun 05

Wx: Clear and partly cloudy.  Winds SW, 74F in the morning, high 80s F later
Seas: Swell out of the SW.  Mostly less than 2 ft.  A few hours were lake-like conditions.
Temp: Warming up – Thermoclines are very noticeable.

 

Buddies were subdude, Jim, and Candy.  We started loading the boat at 0530.  At 0600 I pushed the throttle forward and it broke.  Checked linkage to the carburetor and the transmission and everything was okay.  Removed the panel that holds the throttle handle and found that the threaded metal rod that holds the cable to the throttle cable had broken.  Subdude and I worked the corroded linkage apart and used the remaining 4 threads on the broken rod to put the linkage back together.  After adjusting the linkage on the carburetor to compensate for the shortened throttle rod, we were ready to go.

 

We decided to go far, far away, so we stopped to get fuel at the Pass.  As soon as I put the boat in gear to pull away from the dock, we heard a squeal that was either a belt or a bearing.  We tossed the hook and did some troubleshooting.  Both Jim and subdude have more engine experience than I do, so they took the lead.  A belt that appeared to be plenty tight was slipping anyway, and the guys tightened it even more.  This belt will be replaced soon.

 

Dive One:  Natural Reef.  Top and bottom of the water column were totally different.  On top, the water was a beautiful blue-green, the vis was 30 to 40 ft, and there was very little current.  On the bottom, the water turned brown, the vis was 15 to 20 ft, and there was a nagging current.  There were 2 points of interest.  We saw dozens and dozens of large Jack-knife fish, and I shot a Hogfish.  I have never seen a Hogfish around Destin, and I thought they did not come this far north in the Gulf.  Subdude floated a nice “Fortress” anchor.

 

Dive Two:  Wreck.  Same water conditions.  Shot a Red, a Gag, and a large trigger.  Candy shot many triggers and a nice black snapper.

 

Dive Three:  More broken bottom, but we didn’t find any more fish.

 

Epilogue:  We had planned on 4 tanks, but boat problems kept us from hitting the water until after 1000.  We made port at about 1830 after putting 80 nm on the boat.  I cleaned fish until 2100.  Sure was better than going to work!

 

Date: 18 Jun 05

Wx: Total overcast early and a little rain.  Winds N at 15 kts then SW about 10 kts.  72F in the morning, high 80s F later
Seas: Less than a foot, then like a lake as the wind changed.  Sea breeze picked it back up to a foot in the afternoon.
Temp:  Still warming up – Thermoclines are very noticeable.

 

Buddy was Candy.  I started loading the boat at 0530 and we got underway a little after 0600. The belt that gave us problems on the last trip started to squeal, but it stopped right away.  Unfortunately it stopped squealing because it broke.  We only made it to Postil Point before the engine temp went through the roof.  Of course I had to take another belt off to put the replacement belt on.  Fortunately, Candy found my socket extender that morning and brought it to the boat.  Took about 45 minutes to complete the job.  The broken belt does not even look like it was the right size.

 

The forecast called for a light northerly wind.  I think it was a steady 15 kts.  We decided to stay inshore until the wind died down.

 

Dive One:  Reefex tank.  Nothing special. . . a few triggers and short red snappers.  Candy shot a trigger.  Viz was 15-20 ft.

 

Dive Two:  Wreck.  Candy shot 7 triggers and a red snapper.  I shot 2 triggers and 2 red snappers.  I had gun issues.  I took the sawed-off magnum which I thought I had fixed, but under the load of heavy bands, the trigger mechanism would lock up after each shot.  Vis was 25-30 ft.

 

Dive Three:  Wreck.  More triggers.  Candy shot another 7 triggers and I shot 3.  Another gun problem:  this time I took the big magnum, but the tip broke on the first shot.  I recovered the tip and it has a manufacturing defect (just like the last tip I broke).  I shot 2 more triggers just using the shaft.  Vis was 25-30 ft.

 

Dive Four:  Wreck.  Many red snapper and some were sows.  I shot a nice gag as soon as I left the anchor line.  The tip didn’t come out the other side of the skull, so I wasted a lot of time banging it all the way through and trying to pull it out.  That’s when a 20 lb sow was within pokey pole range.  I shot 2 more triggers and Candy shot another snapper and trigger.  The wreck was incredibly silty and covered in monofilament.  Both of us had to cut free a couple of times.  Vis was 25-30 ft except when the fish started stirring up the silt.

 

Epilogue:  We had a nice tail wind on the ride home and managed 18-19 kts.  Pass was a little rough due to outgoing tide and SW swell, but nothing like the 6-footers we saw 2 weeks ago.  Total trip was about 65 nm, and we were back in port by 1800.  I needed help to load the fish cooler in the car.

 

Date: 1 Jul 05

Wx:  Sunny onshore and isolated rainstorms starting about 5 miles offshore.  Winds SW at 10 kts.  72F in the morning, high 80s F later
Seas: Two feet and less.  Temp:  Still warming up – Thermoclines still noticeable.

 

Buddy was Candy.  I started loading the boat at 0730 and we got underway around 0800.  The bayou and Bay were pretty calm.  We cleared the Pass and headed SW into the wind and swell. 

Got stopped by FWC, but they were friendly (fishing license and cooler check).  We were able to use the radar to head between storms.  Some of the rainfall was torrential.  We tried 3 wrecks and they all had boats.

 

Dive One:  The “Awesome” isn’t so awesome anymore.  It sits in a hole at 120 ft.  Go any direction for 200 ft and the depth is only 90 ft.  The interior of the wreck is full of silt and the hole that it sits in has at least 6 inches of silt.  There were a few flounder, but we didn’t take any.  Vis went from 50 feet at the top to 10 ft (sometimes 0 feet) on the bottom.  As we were coming up the anchor line (still in the bad vis), a school of large fish swam by and I took a “hail Mary” shot.  If I hadn’t been holding the anchor line, I would have been pulled back to the bottom.  I clipped the gun off to the granny line and boarded the boat.  When I pulled up the line, the fish was still attached.  It was a 20 lb Jack Cravelle.

 

Dive Two:  There was only one boat on the Destin Liberty Ship (DLS), so we threw out the anchor.  First dive on the DLS since hurricane Ivan.  A whole section (maybe 40 ft – 50 ft) has separated from the main hull and shoved 20 ft – 30 ft west.  The DLS is terribly over-fished, which is why we rarely dive it.  There are always black snapper around, but we didn’t pull the trigger.  Saw a 6 ft bull shark (there seem to be 2 bulls that hang around the DLS and Whitehill Reef).  Again, vis was 50 ft above the thermocline and about 20 ft at the bottom.

 

Dive Three:  Fort Walton Barge.  This barge has been beat to death.  There are gaping holes in the deck.  The vis was so bad 10 – 15 ft, that I couldn’t tell if I was headed stern to bow or port to starboard.  At one point, I saw a mooring cleat that helped orient me.  Candy actually had to tie off a line real so we wouldn’t get lost.  There was a very large Jewfish (+6 ft) on the wreck.  When he “thumped” me, I could feel the vibration go through my chest.  I had to use the lift bag and all my strength to get the anchor out of the wreck.  If the surface current would have been a little stronger, I would have had to cut the rope.

 

Epilogue:  Uneventful return to port.  Trip was about 70 nm.

 

Date: 3 Jul 05

Wx:  Sunny all day.  Winds SW at 15 kts.  72F in the morning, high 80s F later
Seas: Three feet in the morning, 5 – 6 ft by 1400.  Temp:  Around 72 below the thermoclines.

 

Buddy was Candy.  I started loading the boat at 0645 and we got underway around 0720.  The bayou was pure glass.  The north end of the Bay was smooth, then halfway to Destin Bridge it started getting choppy.  We cleared the Pass and headed straight into a steady 15 kt SW wind and 2 – 3 ft waves (the Marine Forecast and Navy Wave Model were way off). 

 

Dive One:  Dropped on a Reefex tank.  Immediately saw 2 anchors (8 lb and 13 lb Hookers) and attached them to my lift bag.  Anchor rope was hopelessly entwined, so the entire process took at least 10 minutes.  We were only 20 ft from the tank, but couldn’t see it, so Candy clipped off the line reel.  We found the tank, but only one trigger fish.

 

Dive Two:  Barrel Barge.  More bad vis and a smaller Jewfish (about 5 ft).

 

Dive Three:  Broken bottom.  Even more bad vis and nothing to shoot.  Candy picked up some pretty shells.

 

Epilogue:  The wind never let up.  By the time we pulled anchor for the last time, the swell was mostly 4 - 5 ft and white-capping.  There were times when I was standing on the bow, pulling in the anchor line, and the point of the bow nearly went under water as we went from crest to trough.  I thought the Pass was going to be a washing machine, so I headed for the western side of the jetties.  I finally got into position so I could turn NE to enter the Pass with the swell at my stern.  The Pass was bad, but not as bad as I expected.  We were back in port by 1500 and left the boat in the water for July 4th.

 

Date: 16 Jul 05

Wx: Clear, winds SW 10 kts, 74 F

Seas:  Calm in Boggy Bayou and the Bay

Temp: NA

 

Got out of the marina by 0715.  Boat was running great until we were a couple miles into the Bay.  We heard a loud bang followed by unmuffled engine noise.  Dive buddy Jim was driving, so he immediately throttled back and killed the engine.  An inspection of the exhaust system revealed that a fiberglass elbow which is part of the wet exhaust manifold had blown apart and one of the wet exhaust hoses had started to swell.  This was the first indication that the exhaust system had overheated.  We called Towboat US and got towed back to the Marina.

 

Follow up:  Back in port, I removed the elbow and swollen exhaust hose; the inside of the hose was charred and the elbow had delaminated.  This was the proof that water was not cooling the exhaust gasses.  When I ran the fresh-water flush, very little water came out of the starboard riser, but the flow from the port riser looked okay.

 

I replaced the starboard riser and two of the three hoses that make up the exhaust manifold.  When I checked the hose temperature with my infra-red temperature gun, the new hoses were an acceptable 130 F.  Unfortunately, the port hose quickly rose to 260 F.  I believe the old starboard riser was so blocked that water was being forced through the port riser.  When I replaced the starboard riser, the water probably took the path of least resistance and little water flowed through the old port riser.  I replaced the port riser and all hose temperatures returned to normal.

 

Date: 26 Jul 05

Wx: Clear, winds SSW 10 kts, 74 F

Seas:  Glass in Boggy Bayou, calm in the Bay, and less than a foot in the Gulf

Temp:  Bottom finder read 88 F on the surface.  My computer read 83 F on the surface and 73 F on the bottom.  Switched to the three-mil wetsuit.

 

Prologue:  Departed the marina around 0630 and watched the sun rise through the dust cloud that has blown over from the Sahara. . . very pretty.  We headed west to hit some wrecks off of Navarre.  About 10 miles out of the Pass, the engine started missing every few minutes.  I stopped the boat and replaced the fuel/water separator and the problem was resolved.

 

Dive One:  Butthead Tug.  This may be our last dive on the Butthead.  Even though the vis was 40 – 50 ft in the top of the water column, as soon any movement is made near the wreck, the silt comes up and the vis can drop to zero.  The fish in the hold stir it up on purpose, so it’s no use looking for hiding fish.  If you scare a flounder on the outside of the wreck, all you can see is a cloud about 3 ft high, 3 ft wide, and 8 ft long where the flounder use to be.

 

Dive Two:  Navarre Barge.  Not as silty as the Butthead, but the vis wasn’t great. . . maybe 20 ft.  We shot a grouper and a few triggers.  Picked up a beach ball.

 

Dive Three:  Elmore Barge.  The sand has piled so high on the south side of the barge that it is even with the top.  You have to trust your numbers or have a good bottom machine because there is almost no relief.  My machine just shows a thicker bottom line when I pass from sand to steel.  We shot some more triggers and a couple of red snapper.  Picked up another beach ball.

 

Dive Four:  Fort Walton Barge.  Another wreck I may never dive again (unless the resident Jewfish departs).  If the vis is good, it is kind of fun swimming through the inside of the barge.  I don’t know how stable the structure is, and it might not be very safe.  There are no fish to spear because the Jewfish has eaten everything in sight.  Believe it or not, we picked up a third beach ball.

 

Epilogue:  The wind picked up to about 15kts in the afternoon, but the seas never got over two feet.  We made it back to port by 1630.  I parked the boat to have the holding tank emptied, but hurricane Dennis had put the pump-out station out of commission.  When I cranked the engine to pull the boat into the marina, I heard the screeching sound of a loose belt and I watched the temperature gauge start to rise.  The screeching stopped abruptly and the temperature started coming down.  I’m guessing the water pump is seizing and I will probably replace it before next weekend.

 

Date: 30 Jul 05

Wx: Overcast, winds E 10 - 15 kts, 74 F

Seas:  Not too bad in the Bay, but two ft and more in the Gulf

Temp:  Mid 80s on the surface and mid 70s F on the bottom.

 

Prologue:  I replaced the engine water pump on 28 Jul and tested it on 29 Jul.  I got a little nervous when the engine started overheating, but after letting it cool and starting it again (twice), there was finally enough water flowing to get a normal temperature.  My 26 Jul 05 dive report said that replacing the fuel/water separator resolved a rough running engine problem.  Apparently it did not.  I had to empty the fuel/water separator twice before the first dive.  We now believe that we got some bad gas.

 

ECRA Reef Clean-up Dives.  Buddies were Candy and Ed.

 

Dive One:  Reefex Tank.  Vis was less than 10 ft.  We retrieved anchor rope, fishing line, and lead.  I took a speargun just because I know that if I didn’t, I would see a 30 lb grouper.

 

Dive Two:  Another Reefex Tank.  Before Hurricane Dennis, we saw a broken mast with sail attached near this tank.  It may still be there, but the vis was so bad we couldn’t find it.  We retrieved more anchor rope, fishing line, and lead.

 

Dive Three:  Barrel Barge.  Vis was a little better (15 ft).  More lead and fishing line.  There seems to be a Jewfish on every barge within 6 miles of the pass.

 

Epilogue:  The crappy weather finally closed in on us after the third dive.  Actually, my Radar showed that we were surrounded by very heavy rain, but we were able to make it to the Destin Bridge without running into a real squall.  We pulled into the beach on the west side of the bridge (where the Reef Clean-up Party was to be held) and retrieved what left of Candy’s tent canopy.  God bless my son, Stone, for setting everything up in the morning, then trying to save the tent when the storms blew through.

 

From the bridge to the marina, I could only make about 6 kts due to the fouled carburetor problem (although the engine did run smoothly twice which let me get up to normal speed for about 10 minutes).  I guess I’ll be working on the fuel system this week.

 

Date: 30 Sep 05

Wx: Clear skies, winds NE 10 kts early, 72 F

Seas:  Calm in the Bayou and Bay.  Gulf was less than 2 ft early and less than 1 ft by 1600.

Temp:  Did not notice a thermocline.  About 80 F from top to 120 ft.

 

Boat Info:  My last dive report was two months ago.  I reported possible bad gas (there was definitely more water in the separator than usual).  Since my last report, I have replaced the fuel pump, the raw water pump, the ignition coil, the spark plugs and wiring, changed the oil, rebuilt the carburetor, and replaced all of the engine belts.  Although all of this maintenance was necessary, the underlying cause of the original engine malfunction was a loose ground wire from the electronic ignition module (discovered by buddy Jim and Candy).  The improper ground allowed the engine to start and idle, but the engine timing would not advance when throttled up.  Good God All Mighty!  At least we had a couple of hurricanes to keep us busy.

 

Prologue:  We left the marina at 0830.  Buddies were Candy and Jim.  Intel from Subdude convinced us to head offshore.  We saw many (50 or so) small fish floating on the surface.  Although Crab Island looked fairly clean, there appeared to be “red tide” from the Pass out to about 7 miles due south. 

 

Dive One:  Odyssey.  Vis was 20 ft near the surface, but about 40 ft at the bottom.  Shot some triggers, and tortured a red snapper (shot him twice and he pulled off both times).

 

Dive Two:  Belize Queen.  More triggers and a Gag.  We had so much fun that we went into deco and had to hang out for 10 minutes.

 

Dive Three:  Belize Queen.  We went to the Mohawk Chief, but I forgot to load the post-Ivan GPS coordinates.  We did a random search for about 10 minutes, then went back to the Belize Queen.  By now (1530) the wind and current were almost non-existent.  We shot some more triggers, went into deco, and spent another 10 minutes hanging out.

 

Epilogue:  The boat ran better than ever.  The weather remained perfect for the ride home.  We reached the Marina by 1730.  Total trip was about 68 miles.

 

Date: 26 Oct  05

Wx: Sunny all day and low 70s F

Seas:  2 inches (Vortex Springs)

Temp:  68 F

 

Prologue:  We went to Vortex to “dial-in” our drysuits.  All of our adjustments were made while sitting on the entry steps.  We trimmed my neck-seal and adjusted our weights.  Stone (Dacor): 26 lbs; Candy (Moby) 24 lbs.

 

Dive One:  Vortex.  We dove for about 35 minutes. . .  35 incredibly boring minutes.

 

Epilogue:  Diving in fresh water is lovely; however, it is not our “cup of tea”. 

 

Date: 27 Oct  05

Wx: Completely overcast and 60F early, winds NE 10 -20.  70F by 1400.

Seas:  Calm in the Bayou and choppy in the Bay.  Gulf was 1 to 3 ft early and about 1 ft by 1500.

Temp:  No thermocline.  About 75 F from top to 95 ft.

 

Boat Info:  13 Oct 05:  Replaced starter motor, ignition solenoid and associated circuit breaker.  When Candy ordered the parts, she found out the old solenoid and circuit breaker were not “standard” for my engine.  She ordered the correct parts and I installed them.  I also installed a fuel flow meter.  It is working, but will take a few trips to calibrate. 

 

Prologue:  We left the marina at 1000.  Just Candy and Stone on this trip.  Bayou and Bay were uneventful.  When the alternator gauge showed “below nominal” charging, I switched to battery ”1” so I would have a fully charged second battery if needed.  Once through the Pass, there was a strong SE swell competing with a 15 kt NE wind.  We picked the Janet and LCM-8 as targets.  We headed into the swell and could only make about 10 kts without getting beat up and sprayed (there was some white-capping).

 

Dive One:  Janet.  We dove “dry”.  Candy used 24 lbs with her Moby, and I used 26 with my Dacor.  Both suits have a little leakage at the wrists, but I am satisfied.  Candy needs to adjust her CG a little, and she may have an allergy to the latex.  There was a 6 ft nurse shark under the bow, a few small red snappers, and a few baby grouper.  Vis was 50 ft near the top, but only 25 at the bottom.

 

Dive Two:  LCM-8.  Candy switched to her 7-mil wetsuit.  I stuck with the dry-suit.  The LCM certainly looks different sitting upright.  The stern superstructure was fairly intact when it was on its side, but now it’s mangled.  No decent fish seen.

 

Epilogue:  The boat ran great except for the alternator output.  The sun came out at about 1530 and was intermittent for the ride home.  Seas calmed to 1 ft.

 

Just before we pulled anchor on the LCM, we were surrounded by many spotted dolphin.  They appeared to be doing a feeding trick where they would be very active at the surface, then “blow” at the same time and descend.  At first we thought there were only 12 dolphin feeding at a time; however, as they moved away from the boat, we saw their numbers double (must have been 12 up and 12 down).

 

We reached the Marina by 1630.  Total trip was about 39.5 nm (45.5 statute). 

 

Date: 5 Nov 05

Wx: Mostly sunny and 68F early, winds SE 15 - 20.

Seas:  Calm in the Bayou and choppy in the Bay.  Gulf was 3 to 4 ft (a couple of 5s) all damn day.

Temp:  No thermocline.  About 75 F from top to 102 ft.

 

Boat Info:  Since the alternator output was low on the last trip, I decided to replace it.  It took me about 4 hours just to get it off (including trips to the hardware store, auto store, and home to get some specialty tools).  To make a long story short, I had to cut off the head of the pivot bolt, remove the alternator bracket from the engine block (with alternator still attached), and use a hardened steel nail-set tool to drive the pivot bolt out of the alternator and bracket.  I replaced all bolts with stainless.  Next time, it will only take me 45 minutes.

 

Prologue:  We left the marina at 0745.  Candy, Stone, and buddy Jim.  Bayou and Bay were uneventful.  Once through the Pass, there was a strong SE swell and SE wind.  I headed toward the LCM-8 just because it put the bow into the wind and waves.  I could only make about 8 kts into the tightly packed 4 ft waves, so we decided to hit the Phoenix (which is closer).  There was a monkey boat about a tenth of a mile away, so we threw the hook.  The monkey boat pulled up on us and said they were fishing the wreck.  The captain said he had a buoy out, and sure enough, he did.  It’s hard to see an 8-inch buoy in 4 ft seas.  We apologized and pulled the hook.

 

Dive One:  Janet.  Due to the sea-state, we could only turn around (head NW) or continue on to the LCM-8 and Janet (head SE).  A boat was on the LCM, so we dove the Janet.  We dove wet.  I used the 5-mil with 3-mil hooded vest (14 lbs) and Candy used her 7-mil with core warmer.  Vis was a nice 30-40 ft and not much current.  Pretty boring dive until the end.  Earlier in the dive, C